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After de-catting the stock header, knock off 4" megaphones, stage one filter kit, and tuning with fp3, I lost a TON of low end torque. (2015 RGS) When taking off, it is gutless. I heard stories of loss of low end with the knockoffs, but it was pretty bad. Once under way, this thing is way faster than stock, and sounds amazing. I know, I should have went with the real thing. But I already bought them, so I am going to have to use them. I had some thumb screws from another project laying around, so I thought I'd give it a try. Drilling a hole in pipes that aren't working for me wasn't a big deal. I didn't want to drill the stock header, that's why I did it near the inlet of the cans. It helps on drag pipes, so I gave it a try. I'll post my findings when I can take her for a ride.
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